Massive explosion rocks SpaceX Texas facility, Starship engine in flames
Massive explosion rocks SpaceX Texas facility, Starship engine in flames
the explosion, which took place at its Boca Chica Starbase facilities
The raptor testing stand at McGregor experienced an anomaly
Well, which is it? I’m going to trust NASASpaceflight over this article and go with it was a McGregor. No where near Starbase. And that means it will likely have no effect on IFT4 as this article says.
But the headline promised me a “massive explosion” and I’m only reacting to those words. Didn’t read the article, nor did I watch the video to see what actually happened.
“Down with Musk!”
Seriously!
OMG THE SPACEX ENGINE BLEW UP.
Brother yeah, it’s a ground up redesign. It’s brand new. Shit breaks. This article is a big fat nothing burger. and other comments on here being like SEE SPACEX IS DOG SHIT… Just telling the world how uninformed they are with no regard for their own dignity lmao
Just to be pedantic:
IFT 3 was a suborbital flight, so… either it did not reach orbital velocity, or the upper stage careened so wildly out of control that it borked it.
Its kind of confusing as in the live stream of it they keep saying the phrase orbital velocity, reached orbit, but also say it was intended to be a suborbital flight.
Also, the lower stage crashed into the ocean at around mach 2, so maybe that is what they are referring to? Looked like many of the engines did not relight, in addition to significant instability as it traversed back through the atmosphere.
Also also, the ‘re entry’ burn may be referring to attempting to relight the engines while in space? You are probably correct that they mean the landing burn / belly flop???
Its pretty hard to tell actual info about these Starship flights, partially because SpaceX outright lies during their live feeds, is tight lipped about other things, and many sources of coverage are often confused and/or simping for Musk.
One last thing: Does… Starship, the upper stage… even have monopropellant thrusters, or gyros, or anything for out of atmosphere orientation adjustments?
From the IFT3 vid it seemed like either no, or they malfunctioned.
IFT3 was technically suborbital, but only barely. Like a couple hundred km/h short. Literally a couple of seconds longer second stage burn would have put it into a stable orbit. Or the same velocity just with a lower apogee. They intentionally left the perigee just inside the atmosphere so a deorbit burn was not required. This is also the plan for IFT4, iirc. I think they are talking about the bellyflop/suicide burn. It was not planned on IFT3, but is for IFT4.
Both the booster and the ship have attitude control thrusters that you could see firing during the live stream of IFT3. Early prototypes used nitrogen cold-gas thrusters, but were planned to be upgraded to methane/oxygen hot-gas thrusters at some point. I don’t recall if/when they were.
Just to further clarify this…
They did the suborbital thing because they wanted to ensure it came in over the ocean.
If they went orbital, and anything went wrong, they’d have lost control of where it would deorbit and land, potentially putting people at risk.
So sure the rocket did not reach orbit.
No one with even a pinch if knowledge on the topic would ever try to dispute they could have if they wanted.
What you’re talking about is usually referred to as a de-orbit burn. Sure somebody could call it a reentry burn, but not SpaceX. What SpaceX calls a reentry burn is the maneuver when a Falcon 9 booster lights its engines as it first hits the atmosphere to slow down and move the heating away from it’s body. Neither the super heavy booster nor the ship make a maneuver like this.
IFT3 did not make a de-orbit burn, and there is not one planned for IFT4 either.